I managed to get away from the DIY for an hour late this afternoon to test my Raptor 50 after replacing a very bent conrod. All running nice but not a fan of taking off in a good wind, but it had to be done

. Heard a crack on impact. Checked heli, no power on motor, esc to motor lead was disconnected and broke elevator and aileron servo arm. Packed up and went home. Ransacked spares box and found new servo arms. Reprogrammed yge thinking of it as cutting out and re-setup the heli. Ate lunch and went out again. After 1 lipo with no incident, I noticed that the lead connection between esc and lipo was loose ( Im using 6mm bullets)

. So this is the culprit. Anyways, tightened them up by inserteing an allen key inside the bullet to open up the teeth a bit. Agility needs to be adjusted as flip rate and was slow even though I adjusted the dual rates. Turned on laptop, took ages to boot and started to rain. What a day.
Hopefully I will have a better heli day tomorrow. 






. The last flight of the day I managed to tidy up my lazy 8's a bit more and got my turns more consistent. Just need to join them up now and do some circuits.







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