Following crash number 4632, the tail now constantly wags when in a steady hover. It didn't do this before, it happened following a crash.
I've checked the obvious things (no obvious bits missing, tail rotor firmly pushed on, recalibrated the gyro by refitting the battery whilst it's on a level surface) so can I assume I've damaged the onboard stabilization system?
I've checked the obvious things (no obvious bits missing, tail rotor firmly pushed on, recalibrated the gyro by refitting the battery whilst it's on a level surface) so can I assume I've damaged the onboard stabilization system?
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