Always soem niggling issues.
My spectra G got an overhaul about 19mths ago and new fuel lines etc and hen on the second flight and third flights the engine kept dying on flips or loops. After a dozen forced autos I'd had enough and put it away.
I only got it out again a few weeks ago and went through the thing. The replaced hays line had indeed split from the clunk. I also foudn one of the throttle servo standoffs missing - don;t know how I missed that!
Anyway all gone through and sorted again.. last was a leaking tank bung. I ordered an HK alloy set and bung to fit the dubro tank.. fitted that and it still leaked. Taking it off the HK bung had split on tightening..so a new dubro gasser bung ordered and fitted today..no leaks.
Finally a test flight. It took a few puls to start after near 18mths unused but once fird up it purred happily. A simpel set of circuits, some flips and loops and a bit of simpe inverted hovering and everything was fine. I ws just coming in to land after 6 mins to check engine temps and it started misfiring. So back to idle2 and some hovering near the helipad..picked up, stumbled, then dropped to a tickover..another easy auto.
Just been looking at it and it looks like it's stripped the throttle servo gear set (9252)!! that's no biggie except that resetting a gasser curve is a pain.
For all that nice to have had it back in the air unconcerned by wind - just have to keep remembering to take the ticktocks steady with that heavy bus.
My spectra G got an overhaul about 19mths ago and new fuel lines etc and hen on the second flight and third flights the engine kept dying on flips or loops. After a dozen forced autos I'd had enough and put it away.
I only got it out again a few weeks ago and went through the thing. The replaced hays line had indeed split from the clunk. I also foudn one of the throttle servo standoffs missing - don;t know how I missed that!
Anyway all gone through and sorted again.. last was a leaking tank bung. I ordered an HK alloy set and bung to fit the dubro tank.. fitted that and it still leaked. Taking it off the HK bung had split on tightening..so a new dubro gasser bung ordered and fitted today..no leaks.
Finally a test flight. It took a few puls to start after near 18mths unused but once fird up it purred happily. A simpel set of circuits, some flips and loops and a bit of simpe inverted hovering and everything was fine. I ws just coming in to land after 6 mins to check engine temps and it started misfiring. So back to idle2 and some hovering near the helipad..picked up, stumbled, then dropped to a tickover..another easy auto.
Just been looking at it and it looks like it's stripped the throttle servo gear set (9252)!! that's no biggie except that resetting a gasser curve is a pain.
For all that nice to have had it back in the air unconcerned by wind - just have to keep remembering to take the ticktocks steady with that heavy bus.


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