The tail frequency choices are 50/165/270*/333/560hz stock is 270 with the align servo installed I set it at 165hz
The servo is still working fine it responds to all inputs while stationary no problem, adjusting the gain on the tx is working as the lights on the beast x scroll as your adjusting it, the stock gain is 77% with the DX6i and with the heli initialized if you turn the heli 45 degrees it reaches its end point in both directions.
I haven't had the heli in the air since changing the tail servo, when it had the ds76t on it after the original crash it was a little wobbly but that was down to blade tracking and head setup it wasn't all fully dialled in it was just a test flight, then I burnt out the tail servo and fitted first of all a ds76 cyclic and thats when all the problems started it started to wag 7 or so inches left to right then it got to the point where it went to a full pirouette if I compensate on the rudder it doesn't really react until I give it a full input then it spins in the other direction (this is all being done while its on the ground)
I ve made further adjustments over the last couple of days but the weather has been so s**t I've not tested them
my beast x settings:
setup menu
A: default blue
B: default blue
C: default blue
D: 165hz red flashing
E: endpoints set back off from full throw with no binding
F: default blue (reversed)
G: servo arms set at 90 degrees and swash levelled
H: Default red solid
I : default purple (nor nor rev)
J: set with 10 degrees +- ( blade cyclic pitch geometry)
K: still needs adjusting
L: set to their limits and then backed off with no binding
M: default blue
N: default blue
The servo is still working fine it responds to all inputs while stationary no problem, adjusting the gain on the tx is working as the lights on the beast x scroll as your adjusting it, the stock gain is 77% with the DX6i and with the heli initialized if you turn the heli 45 degrees it reaches its end point in both directions.
I haven't had the heli in the air since changing the tail servo, when it had the ds76t on it after the original crash it was a little wobbly but that was down to blade tracking and head setup it wasn't all fully dialled in it was just a test flight, then I burnt out the tail servo and fitted first of all a ds76 cyclic and thats when all the problems started it started to wag 7 or so inches left to right then it got to the point where it went to a full pirouette if I compensate on the rudder it doesn't really react until I give it a full input then it spins in the other direction (this is all being done while its on the ground)
I ve made further adjustments over the last couple of days but the weather has been so s**t I've not tested them
my beast x settings:
setup menu
A: default blue
B: default blue
C: default blue
D: 165hz red flashing
E: endpoints set back off from full throw with no binding
F: default blue (reversed)
G: servo arms set at 90 degrees and swash levelled
H: Default red solid
I : default purple (nor nor rev)
J: set with 10 degrees +- ( blade cyclic pitch geometry)
K: still needs adjusting
L: set to their limits and then backed off with no binding
M: default blue
N: default blue


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